論文

査読有り
2017年10月11日

Thermal analysis of injection beam dump of high-intensity rapid-cycling synchrotron in J-PARC

Nuclear Instruments and Methods in Physics Research, Section A: Accelerators, Spectrometers, Detectors and Associated Equipment
  • J. Kamiya
  • ,
  • P. K. Saha
  • ,
  • K. Yamamoto
  • ,
  • M. Kinsho
  • ,
  • T. Nihei

869
開始ページ
84
終了ページ
94
記述言語
掲載種別
研究論文(学術雑誌)
DOI
10.1016/j.nima.2017.06.028

© 2017 Elsevier B.V. The beam dump at the beam injection area in the J-PARC 3-GeV rapid cycling synchrotron (RCS) accepts beams that pass through the charge exchange foil without ideal electron stripping during the multi-turn beam injection. The injection beam dump consists of the beam pipe, beam stopper, radiation shield, and cooling mechanism. The ideal beam power into the injection beam dump is 400 W in the case of design RCS extraction beam power of 1 MW with a healthy foil, which has 99.7 % charge stripping efficiency. On the other hand, as a radiation generator, the RCS is permitted to be operated with maximum average beam power of 4 kW into the injection beam dump based on the radiation shielding calculation, in consideration of lower charge stripping efficiency due to the foil deterioration. In this research, to evaluate the health of the RCS injection beam dump system from the perspective of the heat generation, a thermal analysis was performed based on the actual configuration with sufficiently large region, including the surrounding concrete and soil. The calculated temperature and heat flux density distribution showed the validity of the mesh spacing and model range. The calculation result showed that the dumped 4 kW beam causes the temperature to increase up to 330, 400, and 140 °C at the beam pipe, beam stopper, and radiation shield, respectively. Although these high temperatures induce stress in the constituent materials, the calculated stress values were lower than the ultimate tensile strength of each material. Transient temperature analysis of the beam stopper, which simulated the sudden break of the charge stripper foil, demonstrated that one bunched beam pulse with the maximum beam power does not lead to a serious rise in the temperature of the beam stopper. Furthermore, from the measured outgassing rate of stainless steel at high temperature, the rise in beam line pressure due to additive outgassing from the heated beam pipe was estimated to have a negligible effect on beam line pressure. The flow and results of the evaluation in this analysis would provide a good indication for both the verification of the existing beam dumps, and the design of beam dumps in new accelerators with higher intensity beam.

リンク情報
DOI
https://doi.org/10.1016/j.nima.2017.06.028
Scopus
https://www.scopus.com/inward/record.uri?partnerID=HzOxMe3b&scp=85025617815&origin=inward
Scopus Citedby
https://www.scopus.com/inward/citedby.uri?partnerID=HzOxMe3b&scp=85025617815&origin=inward
ID情報
  • DOI : 10.1016/j.nima.2017.06.028
  • ISSN : 0168-9002
  • SCOPUS ID : 85025617815

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