MISC

1999年

35年前に施工された在来トンネルの拡幅時における挙動計測

トンネル工学研究論文・報告集
  • 北田 正彦
  • ,
  • 林田 清高
  • ,
  • 櫻井 春輔
  • ,
  • 進士 正人
  • ,
  • 木村 正樹

9
開始ページ
183
終了ページ
188
DOI
10.11532/journalte1991.9.183
出版者・発行元
Japan Society of Civil Engineers

Dramatic traffic increase in modern day necessitated an extension of cross section of Tennozan tunnel, which was constructed by a side drift method 35 years ago, in a very difficult ground condition. Knowing that the initial construction had experienced large deformation and high pressure on concrete lining, a special care was taken for planning and selection of construction method. As a result of the actual extension of the tunnel cross section was completed only with minor deformation with fair confidence in tunnel stability. Displacement recorded for a ordinary section was less than 1mm at the depth of 2m and at most 3mm at surface. That recorded for an extended section, however, went up to 2-3 mm at the depth of 4-5m, and was 10-14mm at surface on the right side.

リンク情報
DOI
https://doi.org/10.11532/journalte1991.9.183
CiNii Articles
http://ci.nii.ac.jp/naid/130004387469
URL
https://jlc.jst.go.jp/DN/JALC/00385835150?from=CiNii
ID情報
  • DOI : 10.11532/journalte1991.9.183
  • ISSN : 1884-9091
  • CiNii Articles ID : 130004387469

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